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The Jaguar 22 was designed by Frank Butler of Catalina Yachts, USA., in 1969 as the Catalina 22, & is still in production in modified form today. That alone speaks volumes for the design. Under the name of Jaguar, they were built as the first of a line, by Eric Birch of Canvey Island, from the 1970s to the early 1980s. It is thought that 1534 were built. CONSTRUCTION As with the 27 & 25, chop stand mat & orthophthalic resins with inner moulding that provides the base for the furniture. The coach roof is balsa cored, & as such can suffer depression under the mast. The deck stepped mast is supported by a kingpost below. Keel is a swing keel lifted by a winch in the companion way. Some also had glass fibre skegs bolted on to protect the hull when drying out. RIG Masthead rig, with fore & aft lowers, all set well inboard. Sail handling is at the mast, & many originally would have had boom roller reefing.. The mainsheet is taken to a horse across the transom. Many rigs by now will incorporate various sail handling modifications. ACCOMMODATION A compact V double berth & infill forward under which, thwartships is the infamous sea toilet, whilst gloriously simple, had no seacock, & if the base breaks will flood the boat. Needless to say many will have been replaced! Coming aft on the port side is a half bulkhead, & a dinette that drops to form a small double berth, opposite of which is seating/long berth. Where the ¼ berth might have been is a clever sliding galley-predating Pegasus boats by several years-which comes over ½ the starboard berth, & inc a sink & usually an excellent 2 burner meths stove. (Origo). Headroom is 4 9", topped by a very large hatch that opens the aft end of the saloon right up. She has plenty of stowage, & a very long cockpit,with a transom hung rudder. ENGINE 4-6hp longshaft outboard on transom bracket. SUMMARY These are truly "little ships", offering surprising accommodation in such a small boat, & excellent coastal sailing. The deep ballasted keel provides stiffness & bite when sailing to windward, indeed I have sailed in the short chop of the east coast in the bottom of a f6 under full sail.(Not recommended, but shell do it!) This boat will inspire confidence in the novice. Also, downwind sailing is enhanced by lifting the keel which still provides directional grip as it lies outside the hull. L Milton
or, Fitting a New Keel to MERIEL (see issue 2 of SEACATS, which also has other
articles about Jaguar 22s) My brother James and myself were looking for a sailing boat since all our experience was with powered boats. Meriel was a Jaguar 22 of uncertain vintage that had sunk at its mooring at Emsworth, Chichester Harbour. The Harbour Master had pumped it out and moved it to Itchenor where we found it with a broken mast. rigging torn from the deck and generally looking very sorry for itself. It had been left on the hard ready to be sold off by Tender. We discovered from the Harbour Masters office that along with the visible damage, the keel was also missing. At each High Tide it filled with muddy harbour water which could later be heard draining from somewhere in the hull. Our worst fears were that in losing the keel it had torn a hole in the bottom and therefore caused it to sink but a bit of probing around revealed a stopcock draining as the tide receded. We hoped this was the reason for the sinking and put in our ultimately successful bid. Meriel was ours. Now all we had to do was move her to a boatyard at Dellquay where the restoration could begin in earnest. But first the leak. At low tide we baled all the dirty water out (and resident crabs), removed all the floating debris and found the suspect stopcock. As expected it was corroded and broken but a wooden bung was quickly knocked in and all that was left to do was wait for the tide to return. To our great relief she floated and a quick tow had her at the boatyard and lifted out. First job was to sort out the keel. We thought that perhaps the keel had broken off where she had been moored but a search of the area by the very helpful Harbour staff at Emsworth found nothing. We guessed it must have fallen off while being towed to Itchenor and was therefore definitely lost. Later inspection of the hull revealed that the keel was bolted on with four bolts to nuts that had been glassed into the hull moulding. This seemed a rather suspect method so we decided the new keel would be bolted right through the hull. The risk of leaking bolts was better than the thought of it falling off again. A few quick phone calls revealed that the cost of having a new keel cast was way beyond our budget so we decided to make our own. I work at a structural steel company so we thought this shouldnt be too much trouble once we had the shape of the keel. By scaling the original drawings that we obtained from Canvey Yacht Builders and measuring every J22 that we could find out of the water (we never managed to see a complete keel) we finally had a drawing of our new keel. This was slightly longer than the original because cast iron is heavier than rolled steel. We figured a bit more depth wouldnt hurt anyway if it fitted the hull slot. From CYB we purchased new bronze keel hangers and pivot pin. With these we made a plywood template to check that our drawing was correct before having the steel keel profile cut. We made the keel 40mm thick which only just fitted the moulded hull slot. A bit judicious grinding of some protruding fibreglass soon had the template fitted. We were now ready to order our new steel keel. The original cast keel had a slight aerofoil
shape to it that we could not replicate with flat steel plate so we faired
the front and trailing edges by gas cutting and a lot of grinding. When
this was complete we then had it hot dipped galvanised for protection.
Now all we had to do was fit it! A scaffold pole was then passed through a hole in the keel that we had cut at the centre of gravity. This enabled us to lift the keel up and then pivot it around the scaffold pole until we were able to place the bronze keel hangers and pivot pin into the correct location under the hull. Four holes were quickly drilled through the hull and into some extra strengthening fibreglass we had built up inside. Ill leave out the details of moving 600lb of steel through the black sticky Dellquay mud! The bolts were coated with sealant and tightened up. Next was to fit an eyebolt for the lifting wire. This was a simple case of drilling and tapping the edge of the keel for the new eye. We did not fancy using stainless steel wire, for lifting the keel, as had been fitted before (it had clearly snapped) so we fitted Dyneema rope which is extremely strong and hard wearing. We changed this after 3 years and it was still going strong with no sign of wear. We fitted a sacrificial anode to each side of the keel as there was rather a mixture of metals present, slapped some coats of primer and antifoul on and our new keel was complete. We have sailed quite a few miles with no sign of problems of leaks or performance. We also have the added bonus of being able to easily check the securing bolts and know it hasnt fallen off again! (See photos of Meriel here) Stephen Horrod |